Optimization and Performance Improvement of Automatic Generation Control (AGC) for 330 MW Subcritical Thermal Power Unit

Journal of physics(2023)

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摘要
Abstract With the continuous assessment of the “Two Detailed Rules”, various power generation groups are paying increasing attention to AGC. A 350 MW subcritical unit has been in a poor performance state under AGC-R mode since the 2022 heating season, with a K 1 value below 1.2 and a K 2 value not reaching the qualified value. It is facing the cancellation of the qualification for AGC-R mode. In the face of the problem with the unit, this article analyzes three reasons. Firstly, the speed setting exceeds the requirements, but the actual unit action does not meet the standards. There is a deviation in power and a significant deterioration in control quality during the turning point and continuous climbing of AGC instructions. Based on the above analysis, this article proposes three renovation plans to optimize the instructions through nonlinear correction functions and achieve the elimination of instruction deviations. It calculates and judges the difference between the corrected AGC load command value and the actual power value of the unit. It calculates the deviation and sends the deviation to a saturated nonlinear link to generate the feedforward of the main turbine control, improving the output of the main turbine control. By setting a variable integral function, the main control output of the boiler is improved. After this technical transformation, the AGC performance of the unit has been significantly improved.
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automatic generation control,agc
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